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	<title>Energy Planning Knowledge Base &#187; Ireland</title>
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	<link>http://casestudies.pepesec.eu</link>
	<description>Over 170 freely available case studies about European energy planning projects.</description>
	<lastBuildDate>Thu, 11 Jun 2009 11:20:49 +0000</lastBuildDate>
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		<title>Wyeth Nutritionals Ireland – Limerick, Ireland. [Building]</title>
		<link>http://casestudies.pepesec.eu/archives/170</link>
		<comments>http://casestudies.pepesec.eu/archives/170#comments</comments>
		<pubDate>Thu, 05 Feb 2009 13:07:43 +0000</pubDate>
		<dc:creator>Adrian Slatcher</dc:creator>
				<category><![CDATA[Energy from biowaste]]></category>
		<category><![CDATA[Ireland]]></category>

		<guid isPermaLink="false">http://pepeseckb.mdda.local/?p=170</guid>
		<description><![CDATA[At the time of project conception, WNI operated three steam boilers consuming approximately 11 million litres of heavy fuel oil per annum and as a consequence generating emissions of sulphur dioxide and particulates.
WNI also generated approximately 115 million gallons of dairy waste water per annum. This waste water underwent full biological treatment prior to local discharge. The micro-organisms essential to the treatment process require the untreated waste water to register within the pH band 6.0-8.5. A fundamental element of the waste-water treatment process within WNI was thus pH-correction of an alkaline waste by the addition of hydrochloric acid. The project was funded in part by the European project and is encrypted LIFE: LIFE96 ENV/IRL/91.
]]></description>
			<content:encoded><![CDATA[<h3>Introduction</h3>
<p>Wyeth Nutritionals Ireland (WNI), a subsidiary of American Home Products Corporation, is one of the largest infant nutritional manufacturing facilities in the world, with European affiliates in 12 of the 15 EU Member States. The Askeaton plant manufactures both powder and liquid infant formulas and employs 500 people.<br />
The project is an innovative system of emission control system for the simultaneous scrubbing of SO2 and particulates from boiler flue gases, giving pH-correction of an alkaline effluent stream and significant heat recovery.</p>
<h3>Objectives and target audience</h3>
<h3>Process</h3>
<h3>Financial Resources and Partners involved</h3>
<p>The total cost of the work was € 853,238 contribution with LIFE amounted to € 359,258.<br />
The beneficiary is: AHP Manufacturing BV, Askeaton, Limerick, Ireland.</p>
<p>WNI identified the potential for applying a single solution to the two problems of atmospheric emissions and effluent pH-correction by combining the two waste streams in an innovative way.<br />
Significant savings in plant operating costs were a potential added benefit.<br />
The idea was to utilise the untreated dairy waste water as a boiler exhaust gas-scrubbing medium in a non-clogging fluidised bed scrubber system. This results in pH-correction of the waste water prior to biological treatment and thus allows a substantial reduction in the volume of acid previously used for this purpose. Finally, the waste heat energy from the boilers is recovered from the exhaust gases, creating additional savings in energy consumption.<br />
The first stage of heat recovery then takes place in economisers, where the heat is removed from the flue gases and put into the boiler feed water. The flue gases then pass through the scrubber tower, where contact with the dairy waste water strips SO2 and particulates from them. The cleaned gases are reheated and exhausted to the atmosphere.<br />
The dairy waste water is circulated continuously over the scrubber tower, with raw effluent make-up and overflow bleed-off. The secondary stage of heat recovery takes place when heat is removed from this liquid and put into the boiler fresh-water make-up system.<br />
The re-circulated waste water becomes acidic following the take-up of SO2. The overflow is discharged to the effluent treatment plant according to pH-correction requirements, thus eliminating the need for hydrochloric acid for this purpose. The particulates are also carried off into the treatment plant, where they are combined with the normal sludge for disposal.</p>
<h3>Results</h3>
<p>SO2 removal<br />
The baseline established at the plant was around 2 400 mg/Nm3. The recognised emissions standard is 1 700 mg/Nm3. The equipment consistently operates at a level below 600 mg/Nm3, which has become a requirement of the integrated pollution control licence at the plant. The system has the capability of 99 % removal of SO2.<br />
Particulate removal<br />
The system removes particulates below mg/Nm3, well in excess of the recognised standard of 30 mg/Nm3.<br />
Energy savings<br />
The system has been shown to achieve energy savings of around 1.4 MW. This equates to savings of around IEP 175 000 per year. There is also a surplus of heat that has no use in this application. In theory, 2.64 MW is available.<br />
Chemical use savings<br />
The management information systems in the plant have proven that the use of HCl in pH-correction has been virtually eliminated as a result of the installation of this system. This generates savings of around IEP 124 000 per year.</p>
<h3>Critical Success Factors / Challenges</h3>
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		<title>Irish Energy Centre &#8211; Dublin, Ireland.</title>
		<link>http://casestudies.pepesec.eu/archives/169</link>
		<comments>http://casestudies.pepesec.eu/archives/169#comments</comments>
		<pubDate>Thu, 05 Feb 2009 12:35:33 +0000</pubDate>
		<dc:creator>Adrian Slatcher</dc:creator>
				<category><![CDATA[Intelligent and energy efficient buildings]]></category>
		<category><![CDATA[Ireland]]></category>

		<guid isPermaLink="false">http://pepeseckb.mdda.local/?p=169</guid>
		<description><![CDATA[The Irish Energy Centre is located on the Forbairt research campus about 3.5 km north of
Dublin city centre. This suburban campus on a gently sloping south-facing site comprises about twenty buildings of various ages, sizes and shapes.
The Irish Energy Centre, a building completed in October 1996, is located on an existing research campus of Enterprise Ireland in Dublin.
This modest building provides flexible and energy-efficient office accommodation for about
thirty people, with exhibition space and ancillary spaces. The two-storey building has a floor area of about 410 m2.
The predicted consumption in the Irish Energy Centre office building is 57% of that of a conventional office building of the same date.
]]></description>
			<content:encoded><![CDATA[<h3>Introduction</h3>
<p>This is a modest two-storey office building (410m2 for 30 people) with exhibition and ancillary spaces. Almost 50% saving on energy use was reached by significantly higher insulation than Irish building regulations. Next to that the high thermal mass, good controlled infiltration and day lighting contributed to the 50% reduction on space heating and electricity use.<br />
The constructions costs for this modest building were just 550,000 Euro for a total of 410 m2 office floor.</p>
<h3>Objectives and target audience</h3>
<p>The green Building Objectives:-</p>
<ul>
<li>To exemplify and promote efficient energy usage;</li>
<li>To provide high quality working conditions for the users;</li>
<li>To make a positive contribution to the existing campus;</li>
<li>To place minimal demand on non-renewable energy sources;</li>
<li>To make an innovative response to traditional materials and energy standards;</li>
<li>To demonstrate that it was possible to achieve these objectives with construction costs not exceeding those of a conventional building.</li>
</ul>
<h3>Financial Resources and Partners involved</h3>
<p>The budget for the entire project, including design fees, was € 635,000. Cost control was a primary concern of the client, and the building was delivered on time and within budgets. Up to now the building has performed to satisfactory.</p>
<h3>Process</h3>
<p>The client (Irish Energy Centre), was a new semi-state agency, the Irish Energy Centre (IEC) was formally established, with the help of the EC Structural Funds Programme, in January 1994. Its role is to promote the efficient use of energy in all sectors, offering advice, information and expertise.<br />
The client wished to construct a building which would itself demonstrate energy awareness in its design and operation.<br />
To this end it commissioned the Energy Research Group (ERG), University College Dublin, to draw up a general and energy performance brief and advise on selection of the site for the project. This work was partly funded under the European Commission’s THERMIE Programme.</p>
<p>The building envelope was designed with U values significantly better than required by the Building Regulations.<br />
With Ireland’s high wind speeds control of infiltration is critical. Before work started on site the contractor was ‘sensitised’ to the importance of workmanship for the energy performance of the buildings.<br />
Energy efficiency was the primary objective of the design, but materials, components and construction methods were selected with their effects on internal, local and global environment in mind. Locally produced recyclable materials with low VOCs were given preference whenever possible. Only new products of which performance was already proven were selected.<br />
The extensive use of concrete in the building&#8217;s construction (ground and first floor structure, some internal and all external walls) provides substantial thermal mass. There are no raised floors or suspended ceilings. Internal wall surfaces and ceilings are plastered and painted, and floor finishes in the atrium and corridor areas are black natural slate to enhance thermal performance.</p>
<p>High levels of insulation and thermal mass with good control of infiltration all help to reduce the heating load. There are also some south-facing windows to the offices and to all cellular spaces.</p>
<p>Limited south-facing glazing, natural ventilation and the thermal mass of the building all reduce the likelihood of overheating. In the office spaces cross-ventilation is manually controlled by openings at each workspace, while the stack effect in the atrium assists the natural ventilation of the areas opening onto it. In the atrium two punkah fans at high level prevent stratification. Reflective metallic venetian blinds mitigate solar gain by 15 to 20% compared with normal internal blinds. Deciduous trees have been planted in the east and west-facing courtyards to screen the sun in summer and filter light in winter.</p>
<p>Windows are evenly spaced and are higher than average (3 m) so that light is cast deep into the room. Glazing on opposite sides of the room provides excellent light distribution. The masonry window reveals are splayed to increase natural light and reduce glare. The atrium brings borrowed light into office spaces to either side.<br />
Energy efficient lamps were specified throughout. Control features include daylight sensors, dimmable light fittings, infrared occupancy sensors and programmable time scheduling. When daylight levels fall below 300 lux the artificial lighting comes on in occupied spaces.</p>
<h3>Results</h3>
<p>During the design stage the winter and spring hourly, daily and monthly heating loads of the building were calculated using the TRYNSYSBIO simulation tool. The results demonstrated that the basic design strategies were effective and were taken into account during the detail design stage.<br />
Day lighting performance in the first floor offices was monitored within the context of the JOULE contract ‘Daylight Europe’.<br />
Under overcast conditions Daylight Factors on the working plane were found to be in the range 5% to 10% and with good distribution.</p>
<h3>Critical Success Factors / Challenges</h3>
<p>Most solid waste generated in the Dublin area goes to landfill sites; in 1993 less than 10% was recycled. It is government policy to reduce municipal waste substantially through increased recycling.<br />
On the Enterprise Ireland campus water supply and drainage are common to all buildings and a large network of underground services ducts runs below the main pathways. Water is metered as it enters the campus.<br />
From the start IEC occupants had in place a paper recycling system. Since 1997 the building has also benefited from a campus recycling / safe disposal system for fluorescent tubes, batteries and similar materials.</p>
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